This weekend, I ran a 480 load of the new blue at a lower pressure (400 psi instead of ~600 like last time). The result:
OH YEAH. The one drawback was that this motor was not nearly as loud and generally “nasty” sounding as the higher pressure one. This was down at a Kn of 180, and operation was completely smooth, coming up to pressure and shutting down cleanly. I like this a lot. I have a 54/1050 and two 38/640s of this stuff ready to go next…
What good is it having a blog without some pretty pictures?
I really need to get out and fly again… haven’t tried since BALLS, I think. Oh well. Here’s some old ones… like here, when things go right… a 98mm N motor with 42″ of propellant (82% solids, 6% Al with a dash of CuO) pushing my school’s rocket “Del Carbon”, made using the techniques I talked about in the composite layups post (yay shameless trackback #2…)

Here’s when things go wrong. We (me and the school group) tried to do a carbon fiber cased O motor, but we had a “peel failure” between the casing layers. The case delaminated and allowed the forward bulkhead to fly out on pressure-up, absolutely torching Les Derkovitz’s rail. We’re still sorry, Les:

Whew. Glad the Flickr integration works well too.
This is the motor that started it all. We got our name at this event, and this motor was the first motor to be fired with the “TDK Propulsion” branding on the flight card. Joe Cox, Charlie Cox, and SpartaChris (aka Chris Williams) built this 12″ Talon, and Todd and I provided the power plant:
The motor worked well, although the rough deployment at apogee caused the casing to be kicked and subsequently damaged upon landing. A new one is ready to go on the lathe, though, so no worries.Lessons learned: